Culprit found finally - cracked coil
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- MegaSquirt Newbie
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Culprit found finally - cracked coil
yesterday i was working on idle and free-rev tuning and after a couple revs, the motor stumbled and died. after trying to crank it over a few times, i was getting fuel dripping out the exhaust. switched plugs, charged the battery overnight. today, same thing when i crank over, 3 cranks and fuel coming out the exhaust. i pulled the upper intake manifold and the back bank has large puddles of fuel on the valves, front bank is fine.
I took a look in my msq and the PWM% was at 75 instead of 100% and length was 25.5. would this cause a bank to get stuck open when running? i double checked the wiring and there isnt a short or leaking injectors....
MSIIV3,2.88,relay board, LC-1,Older Holley 670cfm 2bbl TBI w/85lbhr injectors.
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- MegaSquirt Newbie
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MSIIV3,2.88,relay board, LC-1,Older Holley 670cfm 2bbl TBI w/85lbhr injectors.
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- MegaSquirt Newbie
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- MegaSquirt Newbie
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- Joined: Thu Oct 27, 2005 9:29 am
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- MegaSquirt Newbie
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1) fried injectors not responding correctly in run/start mode flooding the motor
2) bad vacuume source to FPR causing added fuel to be injected
3) some setting somewhere in MT causing obscene amounts of fuel to be injected.
other than that, i have no idea what it could be
MSIIV3,2.88,relay board, LC-1,Older Holley 670cfm 2bbl TBI w/85lbhr injectors.
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- MegaSquirt Newbie
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would having them wired not in parallel or series affect the injectors? i have all 3 positive leads of a bank wired to a single switched 12v and the 3 negatives to a single wire to the relay board.
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- MegaSquirt Newbie
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any way i can test to see if the flyback is dead?Signs of an impending flyback failure are:
* MegaSquirt® will often require higher PWM% over time,
* The engine may start running erratically, especially at higher speeds and loads,
* the injectors may 'stick' open and flood the engine.
That is a good assumption, and a short to ground on the trigger side of the harness would not necessarily be a likely problem.shadowplane676 wrote:if its a short in the wiring, would it have to be a short to ground for the injectors to open? and if i had a short, the injectors are on a switched 12v, so in start/run they have power. However, with the key on or off (not start mode) the injectors do NOT leak at all. its like before MS controls the injectors they are fine, but once MS fires them, they dont close...
would having them wired not in parallel or series affect the injectors? i have all 3 positive leads of a bank wired to a single switched 12v and the 3 negatives to a single wire to the relay board.
I suggested it because it is one of those things that can keep you going in circles if you don't check for it, and it's a simple check. I would suggest doing the check and also wiggling the harness around while you do it just to eliminate it then move on. and check the actual pulse width at the injectors.
'93 Toyota P/U 22RE V3.0 MS2/Extra 3.1.2 Full Sequential Spark and Injection
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- MegaSquirt Newbie
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problem found - injectors staying wide open
1) checked the impedance of all 6 injectors and got ~13.5-14 ohms.
2) checked the wiring to both banks of injectors, no shorts, nothing.
3) removed upper intake and with spark plugs removed, physically watched injectors as the motor was cranked over. I observed the front bank working fine as intended, pulsing squirts of fuel. the back bank (inj. 2 circuit) was going full bore all the time, even to a 4 SECOND spray after the motor was not turning over.
so, what would cause the injector 2 circuit to keep the injectors open 100% of the time even after the MS is powered down? mind you that they dont leak when the fuel pump primes the fuel rail at key on, only once you start cranking.
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- MegaSquirt Newbie
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teh injectors only misbehave during and after cranking, on key-on the FP primes with no injector leaking.
i tested the standard flyback components and the PWM components, but have MS configured for high impedance injectors.
Standard
R33 - 226 ohms
R18 - 265 ohms
D6 - .5v
D20 - .5v
Q3 - .5v
Q11 - .5v
PWM
R30 - 253 ohms
R31 - 265 ohms
R34 - 251 ohms
R35 - 265 ohms
R32 - not present
R36 - not present
Q9 - .5v, 60K+ resistance
Q12 - .5v 60K+ resistance
Q10 - .6v
Q13 - .6v
also, Q1 and Q5 look fine and register open, all solder points are non-bridged. I inspected both sides of the board with a magnifying glass prior to installation in the car.
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- MegaSquirt Newbie
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- MegaSquirt Newbie
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i can IDLE with a VE of ONE and an A/F of 7 to 8 :1, and it will hunt badly but still be running on a VE of ZERO; i cant figure it out. all the wiring is not shorted, is fine but i almost think those back injectors are not shutting again. *sigh* i an totally baffled now. it defies sense. unless there is something wrong with the injector circuits that i cant find or dont know about.
If you mess with the opening times, and go below 1.4, it starts to stumble and try and die, bring it back to 1.4 and it'll run a lil better but its still a crappy, rough, missing idle. changing the VE and req_fuel seem to have no effect on the motor at all.

heres some audio of it - it may help *shrug*

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- MegaSquirt Newbie
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2.3 code
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- MegaSquirt Newbie
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btw, my apologies to everyone, i get frustrated with things when they dont seem to make logical sense, something i still have to work on..
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- MegaSquirt Newbie
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Could you describe clearly and concisely what the problem is?
ok, what happened originally was:
pre-issue) ran well on 2.3 code, drove car round the block until EDIS wheel welds broke. re-welded wheel (properly) and...
1) upgraded to 2.883b code. was working on idle and free-rev acceleration enrichments when after revving the motor a few times, the motor sputtered and started running real bad.
2) Culprit was stuck injectors from 2 year old varnished fuel, since removed and replaced with 4 gallons 93 octane
3)Known good injectors swapped in to replace stuck/gunked injectors, idle has NOT improved, car now misfires badly, and is running extremely rich, even with VE of 1 or 0. Removing Vacuum line from manifold and/or FPR does not effect the motor. changing VE or req_fuel has no effect on the motor either. the only thing i can find that DOES effect the motor is the opening time, which, if it goes below 1.4 it starts hunting, reverting to 1.4 event it out somewhat, but misfires and over-rich condition prevails
you seem to be idling entirely on the opening time, which suggests the PWM parameters aren't right for you injectors, so I would review these very carefully.
from everything i have found, my injectors are high impedance (checked with DMM as well, 13.5-14.2 Ohms) 210cc flow, with similar opening times to the low impedance 3000GT injectors of .7ms each, totalling 1.4ms. MS settings are PWM% 100, Pulsewidth time threshold: 25.4, PW period: 66us
i will re download reload the .s19 tomorrow, and try and post a datalog soon, not sure if the one i have is good or not. will also try and trace the injector circuits
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- MegaSquirt Newbie
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I'm not quite sure what you mean about the 0.7 msec times totalling to 1.4. Injector opening times don't add, maybe you are saying the opening and closing time are both 0.7, and this adds to 1.4? If so, I don't think that's right, for MegaSquirt you want to subtract them (i.e., if the opening time and the closing time are the same, then the fuel pulse width is delayed by the opening time, but there is no net effect on the fuel pulse width). So I think we need some clarification of this.
they are added, .7 to open and .7 to close, which equal 1.4
do you have a fuel pressure gauge? I ask because it is possible that the regulator is sticking and allowing higher than regulated pressures
i have an adjustable regulator with a gauge i have yet to put in. i was thinking about this same issue today and will probably install this tomorrow if the weather cooperates
A backfire can also rupture the regulator diaphragm, leaking fuel directly through the vacuum hose, if you pull the hose off the regulator's vacuum hose off the intake manifold or TB, it should hold suction (and should not have gas in it, of course!).
i checked this yesterday, there IS vacuum through the MAP source hose to the FPR. i have a source Tee'd to both the FPR and the MAP source for the MS. only thing i can think of is that the part going to the FPR got pinched and isnt providing enough vacuum. i will replace this section anyways, as it is only 6"-8" long. there was no fuel in the line as well